"Jim Behning" wrote in message news: snipped-for-privacy@4ax.com...
Well, it appears that timing was the main issue, so I adjusted it by trial and error since there are no marks on the wheel or a pointer in the timing hole. Anyway, I'm at about 85% full-power now. The engine still seems to miss a little bit, but it's not regular. I "fixed" the exhaust leak wih JB Weld and it worked fine for my trip downtown. The leak was limited to a small piece of missing gasket. The exhaust is a little smoky (sometimes not visible) and it kinda stinks. I'd guess this could be due to my timing being a little off? Also, would the converter help the smell. I'm certain that the fuel mixture has been adjusted, so it's probably off as well. Is there any way to test for proper amount of vacuum at the vacuum advance? I don't see this particular test in either of the manuals (I have a Haynes for this car and a Bentley for the older 79 Rabbit). If so, what should the reading be? I hooked up a meter and it moved, but it may be beyond the sensitivity of the guage. It read maybe 1 or 2 inches of vacuum when I revved it up. Just for the record, the car did not run as well with the catalytic converter removed. Besides being obviously loud as hell, there was probably an additional 10% power loss. I don't think I imagined it. So I guess a certain amount of backpressure is necessary? Moot point I guess. And here in NC, my car doesn't need to pass emission inspections, so I might put off buying a new converter ... I would like to formally thank everyone for their input. I read everything and I really appreciate it. Danke schoen.