I was meticulous making sure the filter o-ring was properly seated and that the old oring was not reinstalled. Yes, this is a last ditch effort to get it working properly. 167,000 on odometer seems correct. Pan was never off before (snapped off 4 screws).
UPDATE: I warmed up the engine, then disconnected the cooler line to radiator and connected a hose to it leading to a plastic milk jug. In OD, i revved the engine to about 4,000 then it started to pump out to the jug--the fluid was so hot it melted right through the jug ! brown, filthy crap with gunk in it. did this pump out, refill 4 times unitl fluid was somewhat clean. Now, it won't take off in OD or D, but will in L. Once moving in L, I shift to OD and then it upshifts to 4 and seems to drive OK. Reverse still kicks in around 1,500 RPM. I may have either screwed something up and/or some valve got contaminated? thanks for you help as always, Lugnut !
Since this is a last ditch attempt, first ran a bottle of Transmission Flush Solder Seal part number M1410TF and change the fluid again. Then dump two bottles of a product called TransMedic by SolderSeal part number MS3616. This is not a stop leak product which means it isnt going to swell the seals but a conditioner and I have had some luck with it.
Whitelightning