Update on my 9000 Aero

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A month into ownership the headgasket goes.
But not the very spectacular to see plumes of steam, bad running and=20
massive overheating, oh no, just a build up of emulsified oil in the=20
coolant and a slight rise in temp that made the fan run more often.

So I rings the guy that maintained it for the last two owners and gets=20
it booked in (Saabtec in Glossop) for a HG, a 12k mile service, a new=20
torque bush set (red poly bushes) and get the rear screen washer fixed=20
and drove away in a 9-5 lpt auto loan car.=20

4 days later get a call.
"Yes, the headgasket gone, must have been on way out for a while as that=20
was the very slight oil leak. All done except during the service=20
inspection the rear discs and pads are only about 4k away from=20
knackered. Can replace both for =A3100".

Figured I might as well get them done now, instead of another 2 hour=20
round trip and the required fuel, in 3 months time.

So, all the above, parts and labour =A3600. Shift is nice and tight now=20
thanks the top mount, fan kicks in less thanks to the new coolant, and=20
I'm going to degrease the front of the engine soon and make sure the oil=20
leak is properly sorted.

Nice car again now.
--=20
Carl Robson
Audio stream: http://www.bouncing-czechs.com:8000/samtest
Homepage: http://www.bouncing-czechs.com

Re: Update on my 9000 Aero





Elder wrote:


Re: Update on my 9000 Aero





Elder wrote:

I think there was a problem with bad headgasket for the 9000. I had mine
changed, but that is 100k miles ago, fine since that. Problem was caught
early, so it didn't need head skimming.

Re: Update on my 9000 Aero



johs@sizefitt567777er.com says...

I don't think this one needed a skim either. And the blow wasn't into
the combustion chamber, it was between water ways, oil ways and the
outside world, so I didn't overheat, so it didn't need skimming.

I pulled a litre and half of oil contaminated coolant out and replaced
it with fresh (it had accumulated worst in the header) and was able to
drive it normally for a week until I could drop it off.

I think I caught it early enough to avoid catastrophic failure and
warpage. It didn't even run hotter than normal, and now the
aircon/heater/cooling appears to work a touch better now the
heater/blower circuit isn't pushing hot mayo arround.
--
Carl Robson
Audio stream: http://www.bouncing-czechs.com:8000/samtest
Homepage: http://www.bouncing-czechs.com

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